I might end up getting a right angle jack to help with the strain relief. We’ll see how this holds up.
Yeah…
It hadn’t failed, but was heading that way. I didn’t help that I don’t have any heat shrink large enough to go over the end of that barrel jack. I ordered a pack of right angle barrel jacks from Amazon and soldered the wires in.
Didn’t work. The jack wasn’t long enough or the wrong size to make a good connection to the power source. I wish I had checked connections before soldering the wires on. I ordered a different style of jack in two sizes, 5.5 x 2.1 mm and 5.5 x 2.5 mm.
The 5.5 x 2.5, on the left, turned out to be the correct size. After confirming (multiple times) the positive and negative sides of each connection I slipped on some heat shrink, soldered the wires to the jacket, and blasted flames at the heat shrink.
The right angle is a much better connection because of how the battery sits in the jacket pocket and the extra length will help with strain relief. I feel better about having a soldered connection as well. It’s a win all around.
The pocket where you connect the batter is on the back left, which is an awkward position. In less than two months the wire frayed by the barrel jack.
The exposed wires caused a short in the M12 Power Source, which is the red plastic shell that connects the battery.
The part was dead in the water and gives an error status. What terrible designs in the jacket’s wiring and the power source. Luckily, the battery does have fault protection and still worked. I checked the item on Milwaukee’s web site and other people had the same problems. After leaving a review, it looked like Milwaukee reached out to them. So I left my own review with a picture of the wire…
My partner got the jacket less than 2 months ago. The wire frayed by the connector causing a short, which appears to have killed the power source. I read 12.5v out of the battery just fine, but nothing from the power source. Terrible design in the jacket and with no protection in the power source. I can fix the connection and barrel jack on the jacket without an issue, but not much we can do about the power source.
Their social media team sent me an email the next day…
We are sorry to hear you are experiencing some issue with your M12™ Power Source! As a one-time courtesy, our team would like to assist with a replacement!
About a week later they emailed me again, with a return label to send them both the battery and the power source and they sent us replacements. Kudos to Milwaukee for sending the new version of the power source and a 3.0 Ah battery when the previous one was 2.0 Ah. B will be happy about the extra battery life.
By the time we got both items it was exactly three weeks after I had left my review. I isolated the wires with some cardboard between them so I could make sure the jacket worked with the replacements. It was a success, so I separated the two sides of the wire, tested which side came from which part of the jack, and then cut it off.
I stripped back insulation, put shrink tube around each wire, connected a new jack, put shrink tube around both wires, and gave it a couple wraps of electrical tape.
I might end up getting a right angle jack to help with the strain relief. We’ll see how this holds up.
The range we put in last year tripped the breaker whenever we ran the quick boil burner and oven together. I checked the manual and the unit runs best off a 50 amp breaker, so I finally got around to replacing the 40 amp one along with 6 gauge wire to replace the 8 gauge.
When I first had the idea to do pallet wood walls in the living room, I wanted to create some type of art piece for the wall opposite the TV. I stumbled across this shelf on Etsy when searching for pallet wood art.
After getting rid of my old recliner and lamp (as part of the living room updates) I quickly realized a light was needed for the new loveseat. I thought it would be cool to integrate a light in to my shelf and as a bonus it would be hidden. It would be a fun challenge to work on. Here are the last models I had mocked up in SketchUp before starting on the build.
This initial testing was done using a very simple limit switch, but those are only rated for very low currents and would quickly burn up with the requirements of the LEDs. It took some searching, but I finally found a limit switch that said it could handle 10 Amps of DC. The big controller board for the dimmer and this much bigger limit switch introduced some new challenges to my build.
We picked through the wood leftover from the walls to find an assortment of pieces to use for the backer.
I played around with the arrangement, shortened the length of some boards, and ran everything through the planer to get an even thickness. Then I stained five of the boards and glued the pieces together in several steps.
To make the pull-out part of the shelf I started with a piece of plywood. I cut up scrap sheet metal I’d saved from the drop ceiling light fixtures I removed from my shop several years ago. This would be used behind the LEDs so any excessive heat they produced wouldn’t burn in to the plywood or create a fire hazard. I screwed the metal to the plywood and used some white spray paint on it.
I cut scraps of wood for sides and a divider. Then I cut some slots through them, using the table saw, where the light covers would slide in. I also made a face for this piece, leaving it oversized for now. I attached the sides and front face with glue and pocket hole screws from what will be the top side.
I bought two 10-inch full extension drawer slides and attached them to the top. I filled the pocket holes with plugs and wood filler. Sanding would be done later.
Perhaps the most nerve-wracking step of the project was cutting and positioning a scrap piece of 2×4 to the backer boards. This will hold everything together and allow me to attach the surrounding pieces of the shelf. Thankfully I remembered to cut one end short before glueing and screwing (from both sides) it in place. This is where the dimmer knob and board went. I cut a scrap piece of wood (later replaced with thinner plywood) to prop it up a bit so the knob would be easier to handle.
I put a straight bit in my trim router and cut a channel down the back of the longest backer board. This will be where the power cable runs down and behind the loveseat. It’ll never be seen, so I wasn’t concerned with how it looks.
Next I milled up some boards and glued them to make the top and bottom of the shelf. I tinted clear epoxy with black paint and filled in some holes. I also milled and cut a couple of pieces for the sides of the shelf.
I trimmed all of those to the sizes I’d need. Then I cut rabbets in the sides so the edges of the top and bottom wouldn’t be seen and there would be more support. To fit properly around the dimmer switch I had to notch out some areas and drill a hole for the knob shaft.
I was able to do a dry fit and then had to make a bunch of adjustments to make everything fit better. After a shitload of sanding I stained one coat of Red Mahogany.
The next morning I was able to glue and pin nail the bottom and left side to the backer. The top and right will be screwed in place in case I need to take things apart to troubleshoot or replace the electronics.
After giving the stain several days I masked off the dimmer board and used my paint sprayer to apply four coats of water-based poly.
The next day I put in the LEDs and switch, wiring everything up. I had to make one more piece of wood that would trigger the switch when the “drawer” was pulled out.
I painted the wires white. A bit of hot glue was used to keep them in place and provide strain relief. I also used hot glue down the back side to hold the wire in the groove.
The final step was to figure out where to cut in keyhole slots.
This turned out to be a bad idea. The shelf was just too heavy. So I drilled all the way through the cross beam and drove two long lag screws through and in to the studs.
Here’s a night comparison which shows how bright the LEDs can be.
This video shows everything in action.
This project ended up being a lot more work than I expected. I’m really happy with the results though and we now have a one-of-a-kind piece in our living room.
We got a blackout top down bottom up shade made from SelectBlinds for the window, which came in over the weekend. They’re really easy to install. Now the living room is complete and I can focus on the kitchen remodel.
We bought an old milk can at an antique mall for the corner of the room too.
Two weeks ago, I forgot my mobile charger on a trip up to Rogers City, where I charge with the same type of plug I have in my own garage. After 50 minutes on the road I turned, drove home to pick up the charger, and then had to stop in Bay City to supercharge because I’d already used over 100 miles of range. As I thought about it later that day, since the weather isn’t freezing anymore, I could have made it to my parents’ place with enough range to take a different route home, and supercharge in Gaylord.
Oh well, it was better to be safe than sorry. That night I told myself I wouldn’t let it happen again though, so I ordered a unit I could install in my garage. Then I could keep the mobile charger in the trunk where it belongs.
I also bought a new circuit breaker and wire in order to supply more current (amps) to the unit.
Tesla Wall Connector – $530
25′ of 6/2 Romex Wire – $46
60 Amp 2-pole Breaker – $19
Labor – $0
My total cost was just under $600 since I did the install myself. I’ve read on various Internet forums of people paying anywhere from $300 to over $2,000 for an electrician!
I found a good spot in my garage to mount the plate and ran the wire from there down to the electrical panel.
Installing a breaker and wiring it up can be scary and extremely dangerous, so a lot of people are smart to pay a professional. If you take your time and understand how the system works, it’s quite easy to do though. I turned off the main line and confirmed with a multimeter. The 30 amp 2-pole breaker in the lower right had been used for a hot tub several years ago and wasn’t even wired to anything anymore. I swapped it with the new 60 amp breaker. I closed everything up, turned on the main, flipped the breaker, and voila!
I love when everything works on the first try. Of course, I installed everything to code. 😉
My Model 3 was already charged to 90%, which is as high as you want to charge the car for normal daily driving. I bumped the limit for a quick test and plugged in the car. With a 60 amp breaker, the maximum output of the charging unit is 48 amps, so I was in business. According to Tesla’s documentation, this should charge at a rate up to 44 mi/hr of range. It showed 36 here, but in my experience it takes a few minutes to ramp up and the chargers tend to slow down as they approach the charging limit, so I’ll have to check again after a day of driving. With the mobile charger and a 240 volt 20 amp outlet, my previous charge rate was 14 mi/hr of range, so it’ll be nice to have this boost.
The entire installation took a little over 2 hours since I was working alone and went slow to avoid mistakes.
I drove up to Rogers City for the weekend to work on the charging situation before it gets too cold outside. Last night I plugged into a standard outlet (NEMA 5-15), which should only be able to charge at a speed of 3-4 miles of range per hour, according to Tesla’s home charging documentation. Somehow I was getting 5, which is still really slow.
I brought wire and a new NEMA 6-20 outlet with me, which is the same thing I have in my garage. So this morning we ran a line and installed the outlet. The box in my parents’ garage already had a free 240 volt 20 amp breaker, which made installation a breeze. It took 20-30 minutes for the charge speed to ramp up, which could be due to the colder weather, but I’m getting the same 14 miles/hour I get at home. Much better!
My Dad had this old extension cord. When I looked in the female end I could see a lot of corrosion though. It’s a really long cord and from the feel of it, the wiring is high quality, so I didn’t want to trash it.
Easy upgrade. I cut the ends off and replaced them with new ones, which were about $4 each.
One end of the cable on this cheap charger had worn out to the point where it would only work if held in the exact right position. Or so I thought. After a little rewiring and heat-shrink tubing I found out that it’s actually something on the inside portion of the connector. I’ll have to see if I can open up the case.