A Larger Drill Press Table with a Motor

The table on my new Bucktool drill press is about 9-1/2 inches square, which is too small. I set out to make something bigger. First, a side quest though. I still had the top from my old work table, which was two sheets of 3/4″ plywood glued together.

A big chunk was going to the sanding station, which had sheet metal over junk MDF for the top. The brackets holding it to the metal frame were always getting pulled out.

I cut up the plywood lamination and rounded the corners and edges. I changed the orientation of the machines to give me easier access to the big belt sander, which saved about 10″ of width. I also mounted a power strip.

The small chunk of plywood was for a new drill press table. I worked on the layout, routed the middle for inserts, and routed slots.

The wide slots are for T-tracks. One of my requirements for the table was to make it function with the Magswitch fence I had. So I bought 3/4 x 1/4″ steel bar stock, which fit perfectly through the top of the T-track. The shorts slots in the table offset to the left got additional pieces of metal, allowing me to move the fence over to clear the quill feed handles.

When I bought the flat bar, I place it across both magnets and I could not pull it off. That turned out to be a flawed test. After screwing in the short pieces as shown in that last picture I could easily move the fence. I did some research and found the 1/4″ thick metal was fine, but it needed more surface area to hit the magnetic field. I clamped two pieces of the metal side by side and couldn’t move the fence.

So I bought a piece of 1/4 x 4 x 12″ flat cold rolled steel and cut two 5-1/2″ pieces. Then I did a bunch of sanding and drilling before spraying three coats of lacquer.

On the table, I cut and glued plywood in the back section of the T-track slots. After the glue dried, I routed large areas for the plates. I cut the T-tracks shorter, sanded the table, and gave it 3 coats of shellac. Then I mounted the tracks and metal plates. This turned out to be a much better solution.

It was time to start working on a powerful upgrade. Raising and lowering a drill press table is usually a pain in the ass. This larger table actually got in the way of the hang crank and I wanted to motorize it. I bought a couple high torque gear motors, a momentary 3-way rocker switch, and a 15mm to 8mm flexible shaft coupling.

The crank shaft on the drill press is actually 9/16″, so the coupling was too large (I could only find metric sizes on Amazon). Three small pieces of aluminum can were thick enough to shim it and test. I connected an 18 volt laptop power brick, added extra weight to the table, and toggled the switch. It worked!

I had ordered both the DC90 and DC350 motors and went with the DC90. The beefier motor was too slow and has way more torque than I’ll even need.

I bought a 24v power supply, motor speed controller, fuse, and 12 gauge wire. I also grabbed a toggle switch and limit switches from my parts bins. The toggle switch was so AC wouldn’t be constantly flowing to the power supply. The limit switches were to prevent the table from going out of bounds, which I do enough of on the golf course! I wired things up for an initial test.

When I bought the speed controller there wasn’t much documentation and I was hoping the FWD/REV terminals would allow me to directly connect limit switches. They didn’t. At least not out of the box. The controller has two modes; you can use the switch on the front or bypass it with your own switch connected to those back terminals. In the picture above I got the bypass working with my limit switches and the 3-position switch used in my initial testing.

This was unnecessarily complex, disabled the switch on the front of the box, and meant I’d have to mount the additional switch. I opened up the controller to see how it worked. The case’s switch was plugged in to the circuit board, so I popped off the connector and connected it through my circuit instead. Bingo!

It was a latching switch, but I wanted a momentary 3-position switch, so I bought a pack. I soldered wires to the new switch, clipped a bit of plastic from the case, and fed the wires through the larger hole. The new switch was a perfect fit.

I took the original table off the drill press and brought it to my assembly table. First, I mounted the tables together and then screwed down the power supply. I made a custom bracket for the speed controller.

I forgot about the on/off switch though! So I scrapped the mounting bracket and made a new one. The second one used a piece of metal saved from a table top basketball game and turned out much better.

To make a proper coupling that would join the two shafts I ordered parts from Motion Industries:

The middle piece is flexible and would help with any misalignment, but I wanted to try to get the shafts lined up the best I could. I think it turned out pretty well.

Then I put the table back on the drill press column. After squaring it to the cart, I tightened hose clamps around the rack to prevent rotation. I never need that functionality. Then I figured out the limit switch triggers and positions.

I hadn’t used the drill press much, but while drilling the holes in that piece of butter knife, I was already sick of the cluck key location. So I mounted the clip on the side of the table instead.

I had extra hold down clamps from the assembly table, so I bought M6 star knobs, 100m M6-1.0 bolts, and T-track slider nuts to make them useable for this table. I also bought a 19×12″ silicon tray for the table, to help contain the cutting fluid and chips, when drilling metal.

I forgot to cut corners off the inserts earlier, so quickly did that. It’ll make it much easier to get the inserts out of the table. Eight spares should last a long time.

Here’s a quick demo of the motor and limit switches. This thing is awesome!

This project was a lot of fun and is a big improvement to the machine.

Review: Hychika 3.6V Cordless Screwdriver

Last week I was contacted by Hychika, who asked if I’d like to try one of their tools in exchange for a review. They offered their 20v Drill/Driver, a small tire inflator, or a small cordless screwdriver. I’m set on drills and impact drivers with my Ryobi collection of tools and I don’t have a bike, which would be the ideal use of the inflator. The 3.6V Cordless Screwdriver caught my eye and it arrived in a couple of days.

The set came with an injection molded case, which I usually think are a waste because they’re junk; the parts are always hard to get out and put back in. This case is really no different than my other experiences with them, but for how I’ll use this screwdriver, I’m actually glad to have it. It’ll make the set easy to store in my hobby room.

At only 3.6 volts and 180 RPM, this is not a powerful screwdriver by any measurement. I won’t be driving screws in to hardwood that’s for sure. I’ll keep it in my hobby room where it will get a lot of use working on electronics and small appliances/machines. It’s the perfect size and muscle for that type of use. I did pull it out today when I had to take the face plates off some outlets and was able to remove the outlets too, so it may prove useful in the kitchen or garage when I don’t want to run downstairs for a full size driver.

The kit comes with a USB charger, a mini wrench, and a nice assortment of sockets and bits. The screwdriver itself has a couple of nifty features, like a flashlight, rotating head for use in two orientations, and a quick release chuck. The quick release chuck seems similar to the one on my 18V Ryobi impact driver and I love that thing.

I did a quick search and Ryobi makes a four volt version of this tool, which seems almost identical. Overall this Hychika screwdriver seems like a decent tool for what it’s designed for, but I’m curious how it’ll hold up over time.

DIY Snow Blower Brush & Clean-Out Tool

My new Ryobi snow blower didn’t come with any kind of tool for clearing out the chute, so I came up with my own solution. I also wanted a brush to clean off the snow before storing the machine in the garage, so I grabbed a clearance car brush/scraper from Meijer for just about $4.

I took it to the band saw to remove some of the scraper. I might cut more after using it.

I picked up a couple of 1/2″ PVC couplers from Menards for 29¢/each, so I’d have a backup in case my first idea didn’t work.

I cut out about 1/4 of the PVC, drilled some holes, spray painted it black, and grabbed a couple of zip ties.

It was quick work to figure out where to attach it to the snow blower handle so the brush wouldn’t interfere with it folding open or closed.

Works great! Here’s a quick video showing how it snaps in and pops out.

Update

The foam grip on the brush handle was useless; out in the cold all it did was twist in your hand. I removed it, giving me more surface area to use a second clip, which makes it snap in more securely.

Shop Blow Dryer

My newest tool isn’t one you’d usually think of for a workshop. When B was getting a new blow dryer for her bathroom I asked if I could have her old one. It was dark pink and caked with makeup, but I saw potential. After a simple disassembly, some cleaning, and a new paint job it’s new again.

A blow dryer is useful in a shop when you want to speed dry spray paint, make glue cure quicker, or even create an oven.

6-in-1 Utility Pen

Hitachi had a big booth at Maker Faire Detroit and was giving out these awesome pens. I may have walked by a couple of extra times throughout the day. 😉

I’d never seen anything like these. Some Googling found several variations. Some had a full length ruler instead of the knurled grip seen here. You can get one for $8-10 on Amazon. A bulk supplier, selling a version almost identical to this, has the pens listed for than $2 if you’re ordering a bunch. The features of all of the versions were common:

  • Pen
  • Ruler (inches and centimeters)
  • Stylus (use with a touch screen)
  • Level
  • Phillips screwdriver
  • Flathead screwdriver

Since I got 3 of the pens, I put one in my car, one at my hobby desk, and one at my garage workbench.